果园秸秆覆盖机弹齿式解捆防堵装置设计与试验

    Spring-tooth type unbaling anti-blocking device for orchard straw mulching machine

    • 摘要: 针对果园秸秆覆盖机解捆铺料装置易堵塞问题,该研究基于秸秆解捆过程力学分析,设计了一种弹齿式防堵装置。首先建立防堵装置-秸秆捆离散元模型,通过EDEM仿真比较了加装和未加装防堵装置情况下秸秆扰动情况和出料口秸秆密度变化,阐释了解捆铺料作业过程中秸秆堵塞的形成机制。与未加装防堵装置的仿真结果相比,在刀齿线速度2.3 m/s、秸秆捆前进速度0.05 m/s下,加装防堵装置后出料口内侧秸秆平均密度降低了46%,出料区单位质量流率下的解捆阻力矩降低了28.1%,表明防堵装置可有效降低刀齿扰动区域和出料口秸秆密度,避免秸秆在下料口滞留和高压区形成,进而降低解捆阻力矩。以解捆铺料装置阻力矩标准差为指标开展正交试验,得到最佳工作参数为解捆铺料装置主动辊转速225 r/min、刮板主动辊转速5.0 r/min、弹齿间距100 mm。验证试验表明,与未加装防堵装置相比,185、225和265 r/min三个解捆铺料装置主动辊转速下(刮板主动辊转速和弹齿间距不变),解捆铺料装置阻力矩标准差降低率分别为29.5%、34.0%和30.7%,同时平均阻力矩和峰值阻力矩降低率分别为16.1%和28.5%,所设计的防堵装置作业效果良好。研究结果可为果园秸秆覆盖机防堵装置研制提供依据。

       

      Abstract: Straw mulching has been one of the most essential practices for soil and water conservation, soil fertility, and structure improvement in sustainable agriculture. The current research focused mainly on the mechanism, effect, economic, and ecological benefits of straw mulching. Only a few studies have been reported on mechanization technology and equipment for straw mulching. Previously, an orchard straw mulching machine was developed to realize mechanization. Specifically, the crop straw bales were unbaled and then broken to spread between the rows of the orchard. However, the unbaling-spreading device was easily blocked by the straw, leading to the low quality and efficiency of straw mulching. In this study, a spring-tooth anti-blocking device was developed for the orchard straw mulching machine, according to the mechanical analysis of the straw bale unbaling and breaking process. Firstly, the discrete element model was established for the "anti-blocking device and straw bale" using EDEM software. A comparison was made on the straw disturbance area and straw density variation at the discharge port by the DEM simulation with and without the anti-blocking device. The formation mechanism of straw blockage was explained during the unbaling-spreading operation. The average straw density was reduced by 46% at the inner side of the discharge port. The unbaling resistance torque per unit mass flow rate was reduced by 28.1% in the discharge zone. Specifically, the knife tooth line speed and the feed speed of straw bale were 2.3, and 0.05 m/s, respectively. The simulation results showed that the anti-blocking device effectively reduced the straw density in the knife tooth disturbance area and the discharge port. The straw staying was avoided in the discharge port for the formation of a high-pressure area. Thus, the anti-blocking device reduced the unbaling resistance torque. The optimal working parameters were obtained as 225 r/min for the roller rotate speed of the unbaling-spreading device, 5.0 r/min for the roller rotate speed of the scraper feeding mechanism, and 100 mm for the spring teeth spacing. The verification test showed that the standard deviation reduction rates of resistance torque were 29.5%, 34.0%, and 30.7% under the active roller speeds of 185, 225, and 265 r/min, respectively, in the unbaling-spreading device after the installation of the anti-blocking device. Meantime, the average and peak resistance torque decreased by 16.1% and 28.5%, respectively, indicating the effective anti-blocking device. The finding can also provide a theoretical basis to develop an anti-blocking device for the orchard straw mulching machine.

       

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